Analysis on the Failure Causes of the Collapsed Tubing in an Oil Well

Wu, Jun (2023) Analysis on the Failure Causes of the Collapsed Tubing in an Oil Well. World Journal of Engineering and Technology, 11 (04). pp. 745-755. ISSN 2331-4222

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Abstract

Due to the influence of multiple factors such as internal and external formation and mechanical pressure, medium corrosion and construction operation environment, a tubing collapse failure occurred in an oil well. In order to determine the failure cause of the tubing, physical and chemical tests and mechanical properties analysis were carried out on the failed tubing sample and the intact tubing. The results show that the chemical composition, ultrasonic and magnetic particle inspection, metallographic test, Charpy impact energy and external pressure mechanical property test of the failed tubing all meet the requirements of API Spec 5CT-2021 standard, but the yield strength of the failed tubing does not meet the requirements of API Spec 5CT-2021 standard. Through the analysis of the working conditions, it can be seen that the anti-extrusion strength of the tubing collapse does not meet the API 5C3 anti-extrusion strength standard. The failure type of the well tubing is tubing collapse caused by large internal and external pressure difference.

Item Type: Article
Subjects: EP Archives > Medical Science
Depositing User: Managing Editor
Date Deposited: 07 Nov 2023 12:37
Last Modified: 07 Nov 2023 12:37
URI: http://research.send4journal.com/id/eprint/3234

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